Mr Andrew Low*, Mr Julian Speck*, Mr Andrew
Dacre**
*TWI, Cambridge, CB1 6AL.
**Sassol Synfuels, Private Bag X1000, Secunda, 2302.
Paper presented at Failures 2006, 7 th
International Symposium on Risk, Economy and Safety, Failure
Minimisation and Analysis. 13-17 March 2006. Villa Via Hotel,
Gordon's Bay, South Africa.
The possibility of up rating and changing the service of
existing pipelines can prove to be both financially attractive and
time saving when involved in large project developments. However
the ability to validate and prove that apipeline is safe for
operation involves a variety of mechanical testing, metallography,
fracture mechanics, statistical analysis and good engineering
judgement. The work undertaken will either validate or restrict a
pipeline's future.The paper details some of the test work that
was conducted, and the findings that necessitated some difficult
engineering decision-making to determine the integrity of an ageing
pipeline.
Introduction
Pipelines are most commonly used to transport some form of
product; liquid, gas or both between a set distance and follow a
simple or complex route. It is also true that pipelines are exposed
to some of the worst environmentalconditions, as well as the
possibility of damage through military and terrorist activities.
Most pipelines, however, tend to operate in less hostile
conditions. The financial outlay for a pipeline can consume a very
large part of aproject budget if being built from new. However,
once a pipeline is installed, the operation and maintenance costs
are relatively low and one can expect the pipeline to have an
indefinite. In this event, a pipeline will have to havebeen
designed adequately to satisfy the structural integrity
requirements of its operational life.
It goes without saying that over the expected life of a
pipeline, due to changes in operating philosophies and expansions
of production plants, instances will occur where the duty
(pressure, temperature and product) of the line willchange from
original design. In most cases, re-rating of existing lines makes
the most business sense, however, this requires that various
criteria be evaluated to ensure the integrity of the line.
During a recent major oil and gas development in South Africa an
opportunity arose for such an investigation. A 30 year old 140km,
14in OD x 5.0mm WT, electrically resistance welded (ERW) pipeline
was considered for potential uprating. The pipeline was originally
designed for oxygen service at 60barg was operated for
approximately 16 years at a pressure not exceeding 39barg. In 1998
the service was changed to ethylene and operation continued at
39barg. Theoperator wished to upgrade the system to operate at
50barg and change the contents to natural gas. Significantly, the
re-rating also required that the minimum design metal temperature
(MDMT) be lowered to minus 10°C.Unfortunately, very limited
certification for the pipeline existed as most documents had
previously been destroyed in a fire. If a new pipeline was built
today, the relevant design code would be ASME B31.8 [1] .
Various avenues of investigation were required to establish the
fitness for service of the ERW pipeline.
Experimental Approach
Six 3m sections marked as A1 to A3 and B1 to B3, were selected
from a recent inspection carried out on the pipeline. All six
sections contained an ERW seam weld; sections A2 and B2 also
contained a single girth weld. As identifiedby the operator,
sections A1 to A3 showed corrosion in the body and sections B1 to
B3 corrosion at the ERW seam. Sections B2 and B3 also had an
external coating. It was decided that 6 full scale burst tests
would be conducted on the2.5m lengths, while the remaining 0.5m
ring would provide the material required for all small scale
mechanical tests. A summary of the small-scale tests is shown in
Table 1.
Table 1 - Summary of tests carried out on each section
| Specimen type |
A1 |
A2 |
A3 |
B1 |
B2 |
B3 |
| Tensile (base metal, ERW, girth weld & girth
weld HAZ) |
3 |
9 |
3 |
6 |
15 |
6 |
| Charpy V-notch (base metal & transition) |
21 |
3 |
3 |
3 |
3 |
21 |
| Charpy V-notch (ERW) |
|
|
|
6 |
6 |
6 |
| Charpy V-notch (girth weld & HAZ) |
|
6 |
|
|
6 |
|
| DWTT*
[2]
|
12 |
|
9 |
|
|
21 |
| Fracture toughness (ERW, ERW HAZ, girth weld,
& girth weld HAZ) |
|
6 |
|
6 |
12 |
6 |
Note
* The drop weight tear test (DWTT), specified in API RP 5LR or ASTM
E436, was developed in the early 1960s at the Battelle Memorial
Institute, USA, to overcome some limitations of the
'Pellini' drop-weight test. Drop weight teartesting is a
material characterisation test aimed at avoiding brittle fracture
and ensuring crack arrest in pipelines (seamless or welded).
Burst Tests
The six sections were inspected visually for internal and
external defects and features of interest were marked accordingly.
The sections did have visible defects due to the operational
history and these defects had depths in theregion of 5-10% of the
nominal pipe wall thickness, and 5-40mm in length; often orientated
at an angle to the pipe longitudinal axis.
All six sections were strain gauged at mid-length at 3, 6, 9 and
12 o'clock positions around the circumference, using uniaxial
resistance gauges. For features such as notable internal or
external surface damage, an extra set ofgauges was attached
adjacent to the feature but only on the external surface.
Fig.1 shows internal features noted prior to testing but
examined after testing. Fig.2 shows a case of additional
strain gauging at the site of external damage.
|
Fig.1. Reduced area of thickness, section B3 (inside
surface)
|
Fig.2. Additional strain-gauging at external, section
A2
|
| |
The sections were initially pressurised with water up to 60barg
and at ambient temperature (in the range of 10 to 17°C). They
were held at that pressure for about three hours and finally
pressurised to failure. During thetests, temperature, pressure and
strain measurements were continually recorded.
The lowest failure pressure was recorded in section A3; 116barg
(2.3 times higher than future operating pressure of 50barg),
whereas the burst pressures for the other sections was in the range
of 134.3 (2.69 times future operatingpressure) to 145.1barg (2.9
times future operating pressure). Post-test visual inspection
revealed that the material around the area of rupture was
significantly thinner (about 1.14mm in section B3) than the rest of
the section. It wasnot initially clear whether this locally thinner
material was caused by a result of plastic instability of the base
metal or the area had been present before the test. However,
examination of the metallographic section revealed thatthe flow
lines are interrupted by the lower surface, rather than parallel to
it. This indicates that the thinning was caused by material removal
(erosion or corrosion) prior to the test rather than plastic
deformation during thetest.
Except for sections A1 and B2, all failures were associated with
a pre-existing defect. In sections A1 and B2, the failure occurred
by ductile initiation and propagation parallel to the ERW seam
weld, within the parent material.Only in section B3 did failure
occur from the HAZ. Fig.3 shows the failed section B2,
while Figures 4 and 5 show micrographs of section
B3.
Metallurgical Investigation
Cross weld metallographic sections were prepared using standard
techniques. These were etched in 2% nital and examined using an
optical microscope, taking micrographs as appropriate to document
the bond line, heat affected zone(HAZ) and parent material
microstructure. The ERW sections were then re-polished, etched in
Saspa-Nansa at 65°C and examined in a similar manner. A
macrograph of section A1 etched in Saspa Nansa is shown in Fig
6.
As-received Sections
|
Fig.6. Micrograph of the bond line from section A1,
showing the grain flow
|
With the exception of B2 and B3, all sections exhibited a
similar manufacturing defect, i.e. offset skelp edges (sharp
notch-like features) on the internal surface of the sections. None
of these defects were found at the weld seam.This type of defect is
known to occur in ERW welds and may have been caused by
misalignment of the plates during welding. With the exception of
A3, the depth of the manufacturing defect was always between 5-10%
of wall thickness.
Most samples also exhibited significant grain size differences
between the parent material, the HAZ and the bond line, the latter
often exhibited coarser, non-equiaxed grain (with exception of
section A2). This indicates that theinline seam normalising was not
carried out correctly during production, and did not achieve full
microstructural refinement. This caused poorer material properties
except for section A2.
Burst sections
With the exception of sections A1 and B2, all failures were
associated with some type of surface or embedded defects. In three
cases (A2, A3, B3) local reduction of thickness appeared to have
been caused by material removal, thecause of which is unknown.
Fig.7 shows the failure location of section A2. In section
B1, a large inclusion was found that had penetrated deeply into the
plate. The defect created was not perpendicular to the surfaces,
which probably explains why itsimpact was not significant, in spite
of the fact that the thickness of the material present at the point
where the defect was deepest was less than a quarter of the nominal
wall thickness.
Charpy Impact and CTOD Results
|
Fig.7. Burst section A2, failure location
arrowed
|
Table 2 - Summary of Charpy Impact Tests
Table 3 - Summary of CTOD tests
| Lowest observed Charpy [3] result |
Temperature, °C |
CVN, J |
| ERW bond line |
-10 |
3 |
| ERW HAZ |
-10 |
11 |
| Parent material |
-10 |
22 |
The differences observed in the Charpy results were down to the
grain size in the ERW weld and the HAZ; the latter had a finer
microstructure. This also repeated for the CTOD tests as low
toughness results for ERW bond linespecimens were due to the
presence of coarse-grain microstructures. Finer microstructure for
the HAZ subsequently yielded higher CTOD results than in the bond
line.
| Lowest observed CTOD [4] result |
Temperature, °C |
CTOD, mm |
| ERW bond line |
-10 |
0.007 |
| ERW HAZ |
-10 |
0.018 |
| Girth weld |
-10 |
0.131 |
Fitness for Service Assessments
Fatigue and fracture engineering critical assessments (ECAs)
were carried out to the procedure specified in BS 7910: 1999
[5] . The ECAs considered
pipes with an axial surface-breaking flaw at the ERW weld seam and
corresponding HAZ. It was assumed that the joints were initially
proof tested (on commissioning of the pipeline in 1982) at a
pressure of66barg.
Fracture ECA
The level 2B (material-specific) failure assessment diagram
(FAD) was employed. The lowest experimentally determined values of
fracture toughness for the ERW weld and HAZ at -10°C; CTOD
=0.007mm and CTOD = 0.018mm,respectively, were used in the
ECAs.
From the tests conducted on the 6 sections, the lowest
stress-strain curve and tensile properties (0.2% proof strength of
372.4 and tensile strength of 499MPa) for the parent material at
-10°C was used in the ECA.
Fatigue ECA
A 2.5-month record of cyclic pressure variation in the pipeline
during normal operation was extended over a two-year period, to
estimate typical, future operation of the pipeline before shutdown.
The full cyclic data was simplifiedto a single spectrum, using the
rain flow technique; the pressure drop associated with shutdown and
pressure is associated with start-up periods were also added. The
number of times the pipeline was pressure tested at a pressure
rangeof 66barg, was also considered in the fatigue spectrum. The
resulting 2-year block was repeated to simulate the 22 years of
pipeline in service-life. This simplified spectrum was applied to
the wall thickness case of 4.23mm.
As the product will be transported in a dry condition, the
appropriate fatigue crack growth equation for steel in air, as
recommended in BS 7910: 1999, was implemented.
The worst case ECA is shown in Fig.8.
Fig.8. ECA results for 4.23mm case
Discussion of the results
Upon review of the work conducted it appeared that the results would support the up-rating of the line. The six burst tests demonstrated that leakage or rupture typically initiated in the parent material, at regions of external orinternal damage, suggesting that the seam weld had sufficient integrity, however the poor toughness results could not be ignored. The poor toughness results also impacted the ECA tolerable flaw size calculations resulting in some doubtas to whether they would be picked up during inspection. The ECA procedure includes a high degree of conservatism and some of the assumptions made could be relaxed if more appropriate data were available. If the operator were able toprove that the minimum temperature would be above -10°C perhaps not below 0°C, improvements in toughness could be achieved and possibly improve the ECA results. It was also apparent that the inline seam normalising processcarried out during production was not as effective as it should have been resulting in a less than satisfactory microstructural refinement. This contributed to poorer material properties.
Conclusions
Based on the results of the study the following conclusions were drawn:
- The review of the data illustrated that the area having lowest fracture toughness at -10°C was the ERW bond line.
- The ECA showed the tolerable flaw sizes to be very small, potentially below the limit of detectability of current inspection techniques.
- The lowest rupture occurred at 2.3 times the proposed future operating pressure.
Recommendations
- Appropriate fracture toughness and tensile properties for the parent material, ERW and HAZ could be determined at the minimum design temperature for the pipeline (nominally 0°C), and selected parts of the ECA could be repeated.
- Consideration could be given to alternative methods of demonstrating integrity, such as the application of an in-service pressure test.
Acknowledgements
The authors would like to express their sincere thanks to Phil Robinson and Afshin Motarjemi for their contribution during this work.
Reference list
- 'What is a drop weight tear test?'
- BS EN 10045-1:1990: 'Charpy impact test on metallic materials: Part 1. Test method (V and U-notches)', British Standards Institution, London 1990.
- BS 7448:Part 2:1997: 'Fracture mechanics toughness tests - method for determination of K Ic , critical CTOD and J values of welds in metallic materials'. British Standards Institution, 1997.
- BS 7910:1999 'Guide on methods for assessing the acceptability of flaws in metallic structures'. Incorporating amendment No.1, British standards Institution, 2000.